Needle Bearing
Can you change your own Teflon needle bearing in a Badger airbrush?

Yes,
you can, but it probably doesn't make sense. Badger has the
nice
policy that they will do it free as long as you own the brush, and I've
read that the turn-around time is very short. Besides, you will
have to pay about $4 for a teeny tiny part that's easy to lose or mess
up. Never
the less, I've done it. When I was experimenting with making
fine
lines, I convinced myself that the needle
bearing needed replacement.
SymptomsActually, the main symptoms of a
worn
needle bearing are either pulsing or leaking and very little drag when the
needle is
removed or installed. Normally
you should feel some resistance.
In
a siphon airbrush, the
vacuum
in the paint chamber in the body of the brush can suck air through a
worn bearing and cause bubbles which result in a pulsing in the spray.
To check for this, spray plain water and move the trigger slowly
through its entire range. There should be a continuous spray
with
no breaks. But, if you see breaks, and the brush is the type with
a
floating tip, it is also possible that they are caused by a poor seal
where the tip mates with the airbrush body. To check for
this,
rub a tiny bit of beeswax on this area and try again. If you
still see breaks or pulses, the needle bearing is probably bad.
With a gravity fed brush, you may see paint
leakage
into the rear portion of the body.
Some airbrushes have an
adjustment on the needle bearing. If your's does, that may be
all
that is required.
First Try
I read on the web in a
couple of places that replacing the bearing was no big deal.
So I
visited my friends at Coast Airbrush and picked one up. They
are
reeaaly tiny. (the bearing, not Coast)
To remove the old bearing, I dismantled the brush
except for the air valve assembly. Then I ground the end of a
bicycle spoke nice and smooth and flat and used it to push the bearing
out the front of the brush body.
To install the new one, I
sanded the end of a round toothpick so that it would fit in the hole in
the bearing. I threaded the bearing on the toothpick and
pushed
it in from the front until it was flush with the back of the
paint cavity.
When I re-assembled the brush and tried to install
the needle I discovered the rub. The needle didn't want to go
through the bearing. It was real tight. It turns
out that
Teflon, being plastic can be deformed. I had slid the bearing
on
the needle when it was loose and it felt really nice.
But
the hole in the brush body is a tight fit, and pushing the bearing from
the end caused it to squish a little and become too small for the
needle.
So I e-mailed Badger and begged for help, and a nice man
there e-mailed back with the words "Use a number 55 drill bit".
A
number 55 bit has a nominal diameter of 0.052 inches and the 155 needle
measures about 0.050 inches. It turns out I have a number 55
bit, so I chucked it in a pin vise and carefully reamed out the
bearing. The first try it was still a little too tight, so I
worked it again. Then, HORRORS, it was too loose. However,
luckily I found that by pushing on the end of the bearing again I was
able to tighten it up and now the needle feels and works great.
The
moral of this story? Well, you decide. But if you
decide to
try it, you might end up sending your brush to Badger anyway.
Postscript
Because
I can't leave well enough alone, I eventually managed to damage the new
bearing. It will only take so much reaming and pushing.
So
I drove over to Coast and bought another one. This time I
came up
with a better way to install it. It occurred to me that
reaming
might be causing internal scratches that could lead to leaks.
So
I made the tool shown below.
I
installed the #55 drill bit backwards in the pin vice. Then I
put
a tiny bevel on the exposed end by rubbing it against a diamond stone.
I wanted to eliminate any burrs. The Teflon tubing
is just
slightly larger than the needle bearing, so it acts as a stop when the
bearing is fully in place. The bearing was a snug fit on the
bit.
My theory was that the drill bit being just slightly larger
than
the needle, would prevent the bearing from collapsing during
installation.
Well, it worked pretty well. The needle was
still a bit tight, but usable. However, I discovered that
Teflon
apparently has some memory. The next day, the needle was too
tight. So I removed the needle and pushed the smooth end of
the
bit through the bearing as I twisted it. After a few strokes
like
this, the needle felt about right when I re-installed it.
It's
been a while now, and it still feels and works OK. But, if
this
doesn't do it, I swear I'm sending the brush to Badger to get fixed
right.
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